Home
        Display Specs Page
         Contents
1.  OjCd4x7touo    After the first flights an oil leak was noted  The oil seemed to collect inside the spinner  and spread along the propeller blades  Upon removing the spinner  it was noted that the  plug in the end of the crankshaft was missing  American Aircraft Motors was contacted    and they checked their records  The plug was actually missing  They sent one that  same day free of charge  The plug was installed and the leak stopped     A second minor oil leak was detected around the base or pin of the fuel pump  The fuel  pump was removed and the shaft was tapped in and sealed  The leaking stopped     The next squawk to address was the prop vibration  The prop was removed and  inspected and blade 1 was identified  The lower plug on cylinder  1 was removed and  TDC was detected  Blade  1 was lined up at the 10 o clock position  It still vibrated so it  was sent back to the prop shop  balanced and re painted  The vibration stopped     At five hours of flight time  the engine rings seem to have been seated correctly and oil  temperatures remain stable  The alternator works great and the only failures noted are  the artificial horizon and DG are not working well  They will have to be rebuilt     The turn coordinator stopped working at 6 hours flight time and the tachometer at 8  hours  Replacements have been purchased and installed     The aircraft has now 11 hours of flying time and it is flying strong and straight     The trim cable was seizing and kinked and did not move sm
2. 5 minutes  The weight of part A is  divided by 2 27 and the result is the weight of the distilled water to be added  The water  is added gradually and the viscosity tested with a viscosity cup  Water is added  gradually until a 22 second viscosity is obtained  The resulting paint is filtered and  poured into the paint gun  The gun is set for 22 to 25 Psi with the trigger pulled  The  paint nozzle is opened   turn and the result is a very light fog  The first coat is applied  very thin  The paint nozzle is opened 1 8 turn and the second cross coat is applied after  10 minutes  For the third coat the paint nozzle is opened an additional 1 8 turn and  applied after 10 minutes  The fourth coat requires  4 turn plus 1 8 more and is applied  when the third coat is tacky but does not stick to one   s finger nail  It can take 10 to 15  minutes  The gun is disassembled and washed with water  The paint is set after an hour  and dries overnight          YP TES he  46  4  ge i    Dak FE   ah S       The red and white vinyl stripes were added and the US AIRWAYS decals were applied     Unfortunately  the masking tape should have been the low adhesion type  It pulled the  paint off when we removed it and several parts had to be sanded down to bare metal   primed and painted again     The paint scheme continued to develop and the plane just looks better and better as we  progress     FI       The windshield was cut out of plexiglass and installed  When we were on the last three  screws  it c
3. It will be safety wired after the AD inspection is done  Once in taxi tests   the pump was not working and the top half was replaced with a Airtex model 429 head  which is almost the same but with bigger valves  This was not legal for flight but the  replacement valves were on order  The wrong size valves arrived and had to be  returned  For the flight tests the original pump head was installed with new valves  provided by Antique Auto Cellar  These valves failed in flight after 9 hours and were  found to be made with a new old stock component that was not suitable for current  avgas used  The pump head was returned for replacement and new design valves were  installed  This information was shared with the ercoupe group so other pump heads  rebuilt could be inspected     The right aileron was disassembled  the upper skin was discarded due to corrosion and  wrinkles  The aileron spar was repaired  cleaned  acid etched  alodyned  primed and re   assembled  With two new stiffeners  The obsolete steel counterweight plate was  removed and the reinforcing doubler replaced with an internal alloy doubler  A new top  skin was made and installed  The left aileron was opened up  cleaned  two new  stiffeners installed  the counterweight plate removed and replaced with a new internal  alloy stiffener  It was primed and riveted back together     A whole new wiring harness was made and installed with the VR 600 voltage regulator  mounted on the seat belt carry through triangle  the shunt  s
4. REBUILD OF THE BLUE MISTRESS  N94694      U S AIRWAYS       ERCOUPE N94694    This plane had flown for the last time about 16 years ago  It was owned by Kenneth  Detjen  who worked for the aviation industry in some capacity and who had the intention  to rebuild it  However  he parked the plane due to a fuel leak behind the instrument  panel and never did anything else to it  It had remained in a barn on his property  together with many other projects that never got finished either     Kenneth   s wife died shortly after   met him and his enthusiasm decreased thereafter  He  died not much later     The plane had it   s wings removed and stacked on a frame and the cowl had been  removed to get access to the generator that was missing  The cowl was loose but  covering the engine  Every once in a while someone would turn the prop a few times to  keep the oil moving around the engine so it would not seize up     The windows were broken and the interior was ruined  Instruments were exposed to the  elements and it seemed that the only thing worth salvaging was the propeller     After Kenneth Detjen died his sister wanted to sell the property and asked one of the  local neighbors to take whatever he wanted as long as he cleared he land so it could be  sold  Kenneth lived in an old trailer on the property       purchased the plane from Alton Boyett  who had rescued it from the barn  with the  purpose of salvaging parts   might be able to use for my own plane  The nose gear was  a doub
5. ay  The overlay was  removed and discarded and a new overlay was made and attached  The new overlay is  2 1 4 inches lower to accommodate radios     The fuel tanks were removed  inspected  cleaned out  bubble tested  painted and set  aside for future installation  However  when installed  they leaked and had to be re   sealed and re installed with rebuilt fittings and new gasket    With the fuel tanks removed a thorough inspection of the main spar showed that there  was only minor surface corrosion and that the body of the plane was sound and could  be rebuilt  At this point    had to make a decision  Whether to continue to sell off parts  and discard the rest or to rebuild the plane  It took several months to think about this     am an aeronautical engineer but had never built a plane    had designed a concept  plane and a concept engine but neither were ever built or researched further    have  been a pilot since   was young and had the skills to work with my hands but had never  taken on a long term project like this     After careful consideration and encouragement from both Gene and Armando    decided    could not continue dissecting this plane when   had all it took to be able to return it to  it s former glory  or better       consulted with Armando Montoya  my A amp P  while he was doing an annual on my other  coupe and he encouraged me to do it  He inspected it carefully and pointed out the  items that had to be addressed  He told me much worse planes had been brough
6. d for a new  one as the old one was defective  The brakes were purged and a brake line leaked  The  flare of the brake line coupling was re flared and that stopped the leak  The brakes were  purged and tested again and they finally work     The new floorboards were installed and a new cover for the yoke hole in the floorboard  was made     Serviceable indicator lights for the alternator  landing lights and test were installed     The charging system was not operating on first test  Upon examination it was found that  the voltage regulator was dead  No output detected on the FIELD terminal     After consultation with Fermi ltibayo with ZEFTRONICS  it was determined that the Ford  Alternator STC was wrong and that the correct regulator for this rebuilt Ford Alternator  model C6FF10300 B new number DOFF10300 JR should be a Zeftronics R15V00 Rev  A  with the overvoltage set point at 15 2 Amps as this model alternator puts out 15 3  Amps and not 14 amps  The correct regulator was purchased and installed     Examination of the system also found that the AMP meter was the wrong model to be  used with a shunt  It was supposed to be wired with the full bus power through the  meter  As this is not the safest way to do it  so a Westach model 2A6 15 Amp meter  was ordered for use with the shunted voltage     It is also recommended that the alternator and the regulator have the same ground so  the shielded cable for the field connection was modified so the shield is grounded both  ends  A
7. e landing light fairings were removed from the gear fairings and installed as taxi lights  on my other coupe  New fairings were made with landing lights for this coupe     The engine was removed and mounted on an engine stand for disassembly  The  existing cylinders were removed and discarded  The core was sent to American Aircraft  to be rebuilt  A re ground 10 under crankshaft was located  the camshaft was also  reground 0 10 under and six new cam followers were installed  All new bearings were  installed  The case was inspected and refurbished     The horizontal stabilizer and rudders were removed  The horizontal stabilizer had  corrosion around the mounting bolt tubes so it was set aside for possible future repair   and later discarded     A suitable used horizontal stabilizer was purchased corrosion free together with it   s  elevator which is in better condition than the existing elevator  The elevator required  some repair  With the help of Gene McCay we started to remove the upper skin with the  intention of replacing it but we first tried inserting a doubler that reinforced and  straightened out the kinked area of the trim tab  The existing skin and doubler were  riveted back on     Gene McCay is a pilot and builder having built his own RV8    Again  with the help of gene McCay  the seat structure was removed and rebuilt  The  seat pan was removed and a new seat pan was made and installed with new hinges     The instrument panel was removed and found to have an overl
8. ed the repaired lower engine cowl   Adjusted tension of the elevator and rudder cables again     Installed the baggage compartment cross members  seat back rear panel and made  new marine plywood back panels and floor panels for the baggage compartment  Made  new side panels and installed them with the master switch        Installed the seat pan and seat belts and adjusted belt lengths  Installed seat back  upholstery     Cut and formed two new engine side cowls and drilled for attachment to the top cowl  hinges  Formed two new side cowl stiffeners out of aluminum U channel to replace the  weak L shaped stiffeners that usually break     Painted both wings with final topcoat silver        FINISHED WINGS READY FOR INSTALLATION     Washed  sanded the epoxy primer and primed the fuselage with Stewart Systems water  based Eco Prime     Ordered a new top cowl from Univair to be installed on N87333 and the top cowl of  N87333 will be painted and used for N94694     As the brake master cylinder leaked again    removed it and serviced it with new O   rings  and found a leaky flare on the brake line  The L shaped beam that attaches to the  stringers and the floorboards where the brake pedal attaches was weak so it was rebuilt  adding a stiff plate attached to the stringers with a 3 16    bolt that bolts to the angle  This  arrangement allows for much greater tension on the hinge of the brake pedal without  putting strain on the floorboards  The Brake line still leaked so   removed it a
9. extra 90 degree fitting w as installed to orient the  inlet and outlet towards the hoses and it was installed        Tests prove that it is pumping  At a later date  it was found that this model pump is not  one of the allowed substitutions so new valves were ordered for the old pump and  replaced     The plane currently has the rebuilt old pump with the latest versionof the valves and  works perfectly     DB    ze        US ATRWA         The plane was fast taxied again and showed a strong tendency to pitch up  The trim  was checked and found to be reversed  It was corrected and the fast taxi test resulted in  a 1000 foot hop at low altitude over the runway with very stable handling     The next taxi test was a full takeoff with several turns round the pattern and a very  smooth landing  A second flight was made later that day for 40 minutes where it was  observed that the oil temperature increased to 185 degrees and stabilized  Oil pressure  held good and steady  The vacuum instruments did not operate well  They will have to  be rebuilt  They were donated as serviceable and installed for testing purposes only   The CHT gauge operated intermittently and will be checked  There is an oil leak around  one of the rocker covers  The gasket will be re positioned  The plane handled well  despite gusty conditions  with plenty of power  The alternator charges well and fast     Video of the test flights was uploaded to youtube with the following link     http   www  youtube com watch v
10. h adds the necessary   height to the MLG to keep the plane level with the standard number of rubber donuts  and the single arm nose wheel gear  No spacers required     The brake lines from the spar down were replaced with new lines and an anchoring  plate was fitted at the attachment point between the hard and flexible tubing  This  solves the existing problem where the flexing of the assembly is at the old attachment  point on the hard line causing the attachment bracket to wear the soft metal line     New brake lines were also installed from the T in the center of the spar and all the way  to the brake master cylinder  A new flex hose was installed on the master cylinder and  new hose from the master cylinder to the reservoir     The rebuilt steering mast was installed and the pushrods to the mixer and steering  knuckle on the nose wheel were installed     The rebuilt mixer was installed as well as the bellcranks for the ailerons and the  corresponding new 304 stainless pushrods were installed  These pushrods replace the  old ones that were steel tubes and have a tendency to corrode from the inside out     The elevator horn was installed on the main spar and the cables from the mixer to the  elevator horn were attached     The rebuilt instrument panel with a new overlay was installed and the throttle quadrant  was attached and the trim and throttle mechanisms were connected  New cable and  tubing was used for the elevator trim mechanism     The lower center panel brace was 
11. ing new composite gasket and the relevant nuts were safety wired     The two existing Bendix S4LN20 magnetos were disassembled and cleaned and  serviced according to Bendix Service manual and Bendix Service Bulletin NO 474A with  new points  coils and condensers  The timing adjusted and new Skytronics shielded  harness installed  The magnetos were tested and installed on the engine     The engine breather elbow was removed and cleaned and a 1 1   2    length of brass tubing  was brazed in according to EOC recommendations to reduce oil blow by  The elbow    was re inserted with the outlet facing backwards and slightly elevated to aid in draining  oil back into the engine     The oil tank drain plug was cleaned and a drain tap was installed  It was screwed into  the tank and safety wired  There is no oil in the tank at this time     The gascolator was cleaned and re assembled with new brass fittings according to the  AD   s  and installed on the carburetor  New seals were installed and the required  aluminum supporting brackets were replaced with new ones made out of 316 SS and  installed according to the corresponding AD     The fuel pump was disassembled and cleaned and the fittings re installed with new  brass hose barh fittings  The outlet fitting was plugged with a brass bar  brazed and  drilled with a 1 16    orifice as directed by EOC recommendations to limit the fuel pump  output to 10 gpm  The fuel pump was installed with a new composite gasket  new nuts  and washers  
12. le fork type that   could use and the prop appeared to be serviceable     With the help of Alton we loaded the plane on a trailer and   brought it back to Houston        Once back in Houston  the plane and it   s many loose parts were stored in my hangar     started to evaluate what I had     The existing wings were inspected and intergranular corrosion was found in the main  wing spars which was too extensive to make them airworthy  They were set aside for  parts     After visiting a pair of wings in Denver Colorado that turned out to be corroded also  a  set of healthy replacement wings was located in West Texas with the help of Hank  Gallagher that were corrosion free and were purchased to be re covered        Replacement wings        These wings were cleaned  inspected by Armando Montoya  primed and the leading  edge covered with felt  They were re covered using Stewart Systems process with  Ceconite 120  with water based glue and paints  Once covered and painted  they were  inspected again     Armando Montoya is an AA amp P Al that works for Continental airlines inspecting the big  planes     The double fork nose wheel gear was removed and found to be corroded  It was  replaced by a rebuilt single fork gear  The propeller was sent to a propeller shop to be  inspected  certified and re pitched to be used as a cruise prop  With a 7252  configuration     The tail cone was removed and sold before deciding to rebuild this plane  A  replacement was located and purchased     Th
13. ll other shielded wires are grounded one end only     The final electrical installation schematic is as below with the following exceptions     Dimmer is not installed at this time  The radio light appears to be too dim and may need  to be rewired at a later date     NAV COM is COM only at this time  however  a NAV antenna and coax wiring is  installed            _ INSTRUMENT LIGHTS  Li DG   DIMMER 4       Oi    COH  SO0XL  O  TEMP   OILPRESS     FUEL 7 CARBT          MASTER ON boo   SHIELDED 18 AWG      sy BELLY   STROBES   MAP  ALT IND boo   SHIELDED 18 AWG  A 10  NAV COM XPDR    ao    HIELDED 16 AWG    ALTERNATOR AND REGULATOR TO SHARE A COMON GROUND    ALL OTHER SHIELDED CABLES GROUNDED ONE END ONLY       LAND     lt   Ls  QD     N  3     Cep   I       lt      X                  SHIELDED 6 AWG    PULL START  SHIELDED 6 AWG    BHR CHARGER TERMINAL BLOCK  22 AWG     i   FLD 60 AMP  3 5 AMP BREAKER by a       POS  SUS SHUNT     REG J  IASF      S FIELD SWITCH a  H i wee    4 z ALTERNATOR   50     CAPACITOR  LJ   SHIELDED 14 AwG  gt  SHIELDED 14 AWG       SHIELDED 14 AWG                                     e  _    kz MASTER   zz  22 AWG Uy          SHIELDED 14 AWG  SHIELDED 10 AWG    NOTE  with this installation the wire to the starter is always hot  It is no longer wired  through the master switch which is usually too weak for starter loads     The battery must be disconnected every time maintenance work is being done on the  accessory case or in the vicinity of the starter 
14. made and installed with the retainer for the throttle  cable attached     A refurbished cabin heat box was installed on the firewall and a new pull cable was  installed on the lower right side of the panel and attached     The carb hot air cable and pull to start cables were installed     The existing fuel tank shutoff valve and strainer was installed with an elbow to make  room for the transponder tray  A panel mounted shutoff valve was installed in the line  for easy fuel shut off  The primer was rebuilt installed and connected     A FARIA electrostatic fuel sensor was installed in the left fuel tank in place of the leaky  float type gauge and wired to the electric fuel level gauge on the panel  This fuel sensor  has no moving parts and is intrinsically safe by Eec  And ATEX standards working off  voltage that is too low to be capable of generating a spark  The electronics are enclosed  in a solid epoxy resin puck  Although this device was not approved for aircraft use at the  time  it ha recently been approved for use as of 2010     The existing mechanical oil pressure gauge was cleaned and installed with new tubing     This is the only instrument that was original to the plane     A new WESTACH electric carb temp gauge was installed     A new WESTACH electric oil temperature gauge was installed  All three of the electrical  instruments above were wired to a panel switch and to a 5 amp breaker     A new MITCHELL 60 Amp meter was installed  It was wired to a shunt on the ba
15. nd replaced  it with a long flexible reinforced hose right from the reservoir to the T on the main spar  solving the leaking for good     The lower half of the plane was painted silver with four coats of Stewart Systems water  based paint  Results were extremely pleasing        The landing gear was acid etched  washed and painted white     Once dry  the middle line was masked off and the top half was painted with three coats  of silver blue  After three coats it was evident that the color was too blue  The desired  color should be a grey blue  So we mixed two parts of silver with one part of blue and  produced a better result  The upper part of the plane was lightly sanded and painted  with a very light fogging coat and two more coats of the combined color  The top cowl     top half of the side cowls and top half of the nose bowl were painted with the  recommended four coats with excellent results     The Stewart Systems paint procedure is followed strictly as it is the only way to get  good results  The part A paint is mixed thoroughly until the paint is even and all deposits  on the bottom of the can are mixed in  The part A is poured into a plastic container and  weighed  A maximum of 700 grams is the ideal weight for one application  Smaller  batches are better for painting parts only  The weight of part A is divided by 3 3 and the  resulting weight of part B is added and stirred in until creamy and smooth  The reaction  time starts at this point and the maximum time is 4
16. olenoid and alternator  breaker and strobe unit were installed on the walls of the battery case  Strobes were  installed in the existing NAV lights and wired to the wing junction     Aileron pushrods were installed and connected to the rebuilt aileron bellcranks with new  hardware     The rebuilt horizontal stabilizer was installed with new hardware and the rudder horn  and pushrods installed and greased  The rebuilt elevator was installed and the trim tab  connected to the trim wire  Rudders were rebuilt and installed with new hardware  The  entire empennage was soda blasted  acid etched  alodyned and epoxy primed     The tail tie down was reinforced internally and the tie down and localizer antenna were  installed     The localizer cable was routed to the front but remains un installed as there is no NAV  radio installed in this plane at this time  It is available if one should ever be needed     The intercom was installed and connected to the radio and transponder harness  PTT  wires for pilot and co pilot were installed  the co pilot PTT is on the panel  the pilot PTT  button is on the yoke     Breaker switches for the landing lights and alternator field were installed on the lower  panel pilot side     A tensiometer was borrowed and the tension of the elevator and rudder cables was  checked and adjusted     The brake pedal was found  installed and tested  The brakes did not work  Brake fluid  was leaking out of the left brake  It was disassembled and the O    ring change
17. oothly  It had to be  overcorrected to allow for it to return to a suitable position  The horizontal stabilizer was  removed and a R  C  Allen electric trim actuator was installed in the stabilizer and wired  to a DPDT switch and LED position indicator that was mounted on the quadrant instead  of the manual trim handle     After 26 hours of flight  the oil and filter were replaced and the fuel lines and fuel  strainers were cleaned and   or replaced     The plane now has over 50 hours of flight since rebuilt and no other significant problems  have been detected        Current panel configuration        Landing lights installed on simulated gear doors     
18. racked and had to be removed     A new windshield was cut out of Lexan and installed successfully     The side windows are also lexan and the rear windows are PEPK that is more flexible  and it is installed with the rubber gaskets rather than screwed in so that it can be kicked  out as an emergency exit and not leave any sharp edges like plexiglass or lexan would     With the windows in  the radio and transponder and ELT system were installed and  tested  The map light was installed but not connected yet     The mating plugs on the wings for the strobes were installed  The connectors for the  pitot and staic lines were installed  the ailerons were mounted on the wings with new  stainless hardware     The rear baggage compartment was completed with new upholstery and the seat belts  installed  A plate for the master switch was installed and lexan frames for the  airworthiness certificate and registration will be attached to the rear bulkhead  upholstery     The seat and other upholstery was installed     The wings were installed with new wing bolt kit from Skyport  The left lower main spar  bolt stuck half way in and could not be removed  It was cut off and drilled through so a  hacksaw blade could be inserted and the remaining sleeve cut to the edge  After this it  could be removed easily  A new bolt was ordered and installed  Punch test on the failed  bold proved to be within specifications but the cad plating was too thick  It was cleaned  off before insertion  Notes to thi
19. rvoir was mounted on the engine side of the firewall and connected  The brake  cylinders were fitted with new bleed nipples and the brake lines were purged but not  tested as the brake pedal is missing     The engine case freshly rebuilt by American Aircraft in Oklahoma  was removed from  the shipping crate and installed on the engine mount using new bushings  bolts and  nuts  The two upper bolts were fitted with a bracket with a nut that will allow for lifting  the plane with a 3 point hoist bar     The intake spider and rebuilt carburetor were installed and the throttle and mixture  controls connected  The hydraulic unit covers were installed with new silicone gaskets   washers and locknuts  The four intake elbows were installed with nylon locknuts instead  of the standard plain nuts  Four new Titan cylinders with new pistons and bushings were  installed with new nuts and cylinder base seals  The existing pushrods turned out to be  too short and a set of  070 pushrods was ordered from Fresno and installed     The starter and alternator were installed using new gaskets  nuts and washers  The old  fuel filter screen was de soldered as instructed in the STC for the spin on filter adapter  and a bushing to adapt the new temperature sensor probe was soldered in using silver  based solder  The modified filter housing was installed on the engine using a new crush  washer     The oil suction tube was installed with a new crush washer and safety wired  The oil  tank was installed us
20. s effect were shared with the EOC group and the  supplier of the bolts  Anyone using these bolts is recommended to remove the cad  plating first     The N numbers were installed and the regulatory placards also  A new identification  plate was engraved to be installed on the airframe  The original data plate is safely  stored with the logbooks     The aileron pushrods were connected and found that the ailerons are about 4    too high   The push rod lengths will be reduced to get the ailerons level with the trailing edge of  the wing at the walkway     The strobes were connected and tested  One works and one doesn t  The wiring was  checked and corrected for polarity     New polished wing gap covers were made and installed with 8 32 screws  The wings  were fitted with nutplates to avoid using sheet metal screws     Armando Montoya came out and checked all of the AD   s     The header tank was loaded with one gallon of fuel and a fast taxi test was done  The  plane tracks well with no shimmy  the yokes are level and the brakes improved after a  few runs  The main tanks were loaded with six gallons of fuel and it was found that the  mechanical pump was not pumping fuel into the header tank     The fuel pump was removed and found to have one bad check valve  Since these check  valves are hard to find  a complete Airtex model 429 was purchased at an auto parts  store and the top chamber was removed and installed on the lower section of the old  pump  The bolting is compatible  an 
21. s the original spar with the spar reinforcement in  place        NEW REAR SPAR INSTALLED  NEW WALKWAY TRIANGLES          By replacing the spar beam and re attaching the original spar fitting  this qualifies as a  repair and not a replacement     There was also considerable corrosion in one of the triangular wing walk reinforcement  triangles so it was also replaced with a fabricated piece made by Aircraft Components  of Houston     The new bottom skins were fitted with most of the original reinforcement strips  new  ones were added as needed and primed where the two metal surfaces are in contact     The new skins with new inspection ports were installed on the airframe        NEW REAR BELLY SKIN TRIANGLES WITH INSPECTION PORTS          NEW CENTER SECTION BELLY SKIN POSITIONED AND RIVETED     Once all of the belly skins were riveted in  the bottom was acid etched  alodined and  primed with epoxy primer and the drain holes were made and angled backwards in  order to create a suction when in flight     The main landing gear was completely disassembled and cleaned  and re assembled  with new grease and locking devices     The brakes were disassembled and cleaned  the right brake was discarded and  replaced with a serviceable brake  New clips were installed using large POP rivets  instead of the pins that have a tendency to fall out     The bearings were greased and new Desser monster retread tires were installed with  new inner tubes  These tires have an extra inch of rubber whic
22. stiffeners were installed to replace the corroded steel counterweight pad  riveted back  together and painted     Four new ECI TITAN C 85 cylinders with Nickel Carbide barrels were purchased from  ECI in San Antonio  The existing rocker arms were sent to be serviced by ECI     A new set of spark plugs was purchased as well as a spin on oil filter kit  Both of these  were taken to Argentina and sold to local Ercoupe owners  A second spin on adapter  was re ordered and installed     A rebuilt 60 amp FORD  Cessna alternator and new Zeftronics V600 voltage regulator  was purchased for later installation with a new drive gear and vibration damper  The  shaft of this alternator failed and a new rebuilt alternator and gear set was purchased     The battery box was rebuilt and painted with the solenoid  shunt resistor and alternator  breaker mounted and wired to the sides  The starter cable was the only electrical cable  to be re used and all the rest of the wiring is new     A row of switches was mounted on the panel next to the breaker switches  The breaker  switches were then relocated to the bottom of the panel and the location of the breakers  was used to install a new volt meter and a CHT gauge  A rotary switch was installed on  the bottom of the panel to select cylinders for the CHT gauge     The brake master cylinder was rebuilt twice with new O rings and fittings  The brake line  flexible hose is new and the floorboard bracket was rebuilt and installed  The brake fluid  rese
23. t back  to life  This one was too good to let it fade away     Following his advice  the belly skins were removed and used as patterns to cut new  belly skins  New central skin and the two triangle shaped skins were made with new    alloy one gauge thicker  They now match the same gauge used on later model Forneys  and Alons that do not have the beads and the problem of belly skin wrinkles  Two new  wing walk lower skins were also cut and the reinforcing ribs of the old skins were re   used wherever possible and new ones were made and installed instead  To enable  inspection of the rear spar  inspection ports were installed on the skins after adding  doublers as recommended by the corresponding AD  Although it applied to the thinner  skins  it seemed like a good idea anyhow        CORRODED BELLY    SKINS BEFORE REMOVAL    Once the plane was set up on it   s firewall with the tail straight up and secured to the roof  rafters  a closer inspection was made of the rear spar  There was not only corrosion  present but also a wrinkle and crack at the attachment point of the right rear spar  The  rivets were drilled out and the whole right rear spar was removed and sent to a certified  shop to be reproduced but in 0 52 gauge alloy  One gauge thicker and consistent with  the thickness used on Alons  The thicker spar no longer requires the spar reinforcement  kit  The wing attachment fitting was re attached  the spar was positioned  clecoed and  riveted into place  The left spar remain
24. terminal     The above drawing does not include magnetos  radios  intercom  transponder  ELT or  GPS wiring diagrams        GENERIC ERCOUPE WIRING DIAGRAM  FOR 60 AMP ALTERNATOR       A  FAIRCLOUGH                                  PARTS LIST    BATTERY 2 VDC 36 AH CONCORDE   STARTER 2VDC DELCO REMY PULL START   ALTERNATOR 6 YDY 60 AMP   FORD CBFF10300 B REBUILT NUBER  DOFF10300 JR  VOLTAGE REGULATOR 2 WDC ZEFTRONICS R15V00 REV A  BATTERY SOLENOID 2 VDOC   SHUNT 2 wDC WESTACH 237 60   AMP METER 2 DC 60 AMP   WESTACH 2AB 15  VOLT METER 2 DC   OIL TEMP GAUGE 2 wDC CHIEF ISS CAOT M  OIL TEMP SENDER 2V0C CHIEF   OIL PRESSURE MECHANICAL   FUEL LEVER 2VDC FARIA   FUEL LEVEL SENDER 2 YDC FARIA ELECTROSTATIC   CARB TEMP GAUGE 2 VDC WESTBERG   CARB TEMP SENDER 2 WDC WESTBERG   COM RADIO 2 WDC KING KX 126  APDR 2 VDC KING KT 170  INTERCOM 2V0C SIGTRONICS SPO 400  ENCODER 2  0C   GPS NAY 2 WDC AIR NAYW EKP IV                                  The seat belt triangles were installed as well as the seat back  The seat pan is out at  this time     Disconnected the chain on the steering column  centered both yokes in horizontal  position and re installed and tightened chain checking for the centered position of the  spider and aileron pushrods and rudder positions  The nose wheel is also centered   Final adjustments of the rudder cables  ailerons and nose wheel can be done after taxi  test     Installed the handbrake cable  brake pedal and floorboards   Sanded and primed the nose bowl  Install
25. ttery  box     A new altimeter was installed and connected to the static line   A new airspeed indicator was installed and connected to the pitot line   A new VSI was installed and connected to the static line     A rebuilt electric turn and bank instrument was installed and wired to a switch and the 5  amp breaker     A rebuilt artificial horizon was installed and connected to the venturi line   A serviceable DG was installed and connected to the venturi line     A serviceable vacuum gauge was installed in the panel and connected to the venturi  line     A new instrument air filter was installed and connected to the venturi line     A rebuilt RPM   Hobbs meter was disassembled and adjusted to reflect 749 99 hours    the higher of the engine time registered with the FAA and time shown on the old Hobbs  meter   and installed in the panel  This RPM meter failed and was replaced with a new  one  The tach cable failed in flight later and was also replaced with a new one     An AIR GIZMOS docking panel for the AvMap EKP IV GPS nav system was installed   The cleaned and rebuilt mechanical clock was installed in the panel   A serviceable magnetic compass was installed in the panel     A serviceable ELT remote monitor switch assy  was installed in the panel        UNFINISHED INSTRUEMNT PANEL ELECTRICAL WIRING TEST    A pair of used ailerons were located in Michigan and purchased  One had to have a  new top skin installed and the second one was opened  cleaned  primed  two new alloy  
    
Download Pdf Manuals
 
 
    
Related Search
    
Related Contents
  LEC R50263    Collecting and Preserving plant specimens, a manual  Motorola 6803578F47 Bluetooth Headset User Manual  COFFEE QUEEN - Crem International  Warehouse of Tiffany TS47+BB75B Instructions / Assembly  user manual  Modèle Felicitas / BM 702 Mode d`emploi      Copyright © All rights reserved. 
   Failed to retrieve file